
Design and development of a prototype slashing machine for plantations in developing countries.
Despite the present vast exploration of raw minerals in Papua New
Guinea, it is still predominantly an agricultural country with 80 per
cent of the population sustaining their livelihood through it. This is
by cultivation of food crops and cash crops as coffee, tea, cocoa,
rubber and copra. Apart from gold and copper, agriculture including
forestry is the country's largest exporter representing over 35 per cent
of the total earning.
Most of the cultivation are in cash crop plantations. The cocoa and
coconut plantations are mostly located on the coastal and island areas
of Papua New Guinea while the tea and coffee are in the highlands. Since
the introduction of commercial plantations in Papua New Guinea, very
little has been done to improve the slashing methods. To this date, the
slashing of the weed regrowth in the plantations is still dine manually.
Although herbicides are available, the cost is still beyond the reach of
most small holdings. With the slashing of the plant regrowth as the most
frequent activity in the plantations, a Prototype Portable Slasher was
designed and developed to assist with this task. The development of this
machine was aimed at increasing the overall efficiency of the slashing
process in the cash crop plantations.
Before the design and development of the Prototype Portable Slasher, an
investigation of the mechanical properties of common plantation grasses
in Papua New Guinea was conducted. These mechanical properties of grass
stems in Papua New Guinea were gathered using a Stem Impact Cutting Rig
designed and built at the University of South Australia. The cutting
information from the plant stems was analysed and then used as a basis
for the design of the Prototype Portable Slasher. The Prototype Portable
Slasher was then designed and built at the School of Manufacturing and
Mechanical Engineering, University of South Australia. The machine was
tested and evaluated at the Papua New Guinea University of Technology,
Lae.
A laboratory and field tests were conducted during the preliminary
trials on the Prototype Portable Slasher. Modifications were done to the
portable slasher and its components to rectify problems encountered in
the trials. These modifications include the selection of a new 24 cc
engine and the usage of aluminium engine holding frame. Consequently,
the overall weight of the engine assembly is 3.6 kg which has been
reduced by almost fifty per cent. Furthermore, this has also
significantly reduced the strain on the operators and has eliminated
slippage of the strap plug. In addition, the extension spring was
modified with reduction in the free length to 306 mm and also the number
of coils reduced from 176 to 136. This resulted in constant spring
tension to support the weight of the engine assembly.
The above modification were made as the result of several design
problems encountered during the preliminary trials. The laboratory tests
detected a major problem with the fabric strap assembly due to the
partial stitching of the strap socket. This problem further contributed
to the slippage of the strap plug because the strap assembly was not
vertically aligned with the operator's waist. Likewise, the fabric strap
assembly was not able to fully support the machine when it was attached
to the operator. The strain of the back of the operator was a main
problem observed during the trials. This was due to the weight of the
engine assembly. These situations were considered and modifications were
done to rectify these problems as discussed earlier.
Apart from this problem, the Prototype Portable Slasher performed very
well during the field trials. The Cutting Force per unit area ranged
between 3 N/m2 and 7 N/m2 and a Cutting Energy ranged from 3kJ/m2 to 6
kJ/m2. The average fuel consumption per area is 4 ml/m2 and average
cutting time of 0.5 minute/m2.